Gary pope
Active Member
New find I just got back from picking up a 94 XP with the 657 exit motor in it. The guy that I got it from stated to me that it would start up fine and run real good, but after an hour of riding it get back to the DAC take a break for a little bit and then he tried to start it and it wouldn’t crank over really really slow. What could be causing it? He stated that it was a new battery at the time and that all the connections were cleaned from the battery To the motor. Any thoughts?