Afternoon all and appreciate all the help getting this far. Finished the full fuel system replacement, oil exchange and prime as well as Mikuni carb rebuild kit. Popoff pressure test was good at 28 and 29 respectively as was the vacuum test outlined in the carb rebuild thread so buttoned those up and put everything back together. Fired her up and she was revving what seemed super high and when you blip the gas or rev it is has a slight note change and may elevate just a touch in RPM if at all. Not looking to burn it up so checking here first. Carbs are set to factory settings for low and high. Backed off the idle screw to the point where it wasn't touching any more and reset to just touching.... same result. Should the lower butterfly be snug to the walls at idle or should it have a little bit of a gap (1/8th to 1/16th" maybe is the closed position from where its currently set working off the way it was). Was about to head out to the river for an inaugural test but looking like that may not happen. Have to head out by morning either way so any suggestions? RV and oil pump bracket seem super snug as do the carbs so while air leak could be a culprit not certain. Thanks