darrylmccaw
Member
I just re-built my carbs on my 94 GTX, before they were rebuilt it bogged and wouldn't go anywhere!
I put new needle and seats in (2.0), checked the pop off pressure and it was about 23-26 in both carbs.
I also replaced all of the fuel hoses and have bypassed the fuel selector valve and the stock fuel filter (I put an inline filter on).
I turned out the low adjuster 3/8 and the high 1 1/4 as per Sea Doo PWC Carburetor Reference
This weekend I had it out, really hard to start (had to have throttle wide open and choke had no effect) and it idled rough and at low speeds it was terrible. Once you hit about 1/4-1/2 throttle, it took off like a jet and ran significantly better then before I rebuilt the carbs (more power and plenty responsive).
Any suggestions would be great before I take it all apart again!
Thank you all!
I put new needle and seats in (2.0), checked the pop off pressure and it was about 23-26 in both carbs.
I also replaced all of the fuel hoses and have bypassed the fuel selector valve and the stock fuel filter (I put an inline filter on).
I turned out the low adjuster 3/8 and the high 1 1/4 as per Sea Doo PWC Carburetor Reference
This weekend I had it out, really hard to start (had to have throttle wide open and choke had no effect) and it idled rough and at low speeds it was terrible. Once you hit about 1/4-1/2 throttle, it took off like a jet and ran significantly better then before I rebuilt the carbs (more power and plenty responsive).
Any suggestions would be great before I take it all apart again!
Thank you all!