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1994 GTX carbs rebuilt - no high end

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ueww40

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I just got through rebuilding the dual carbs on my 1994 GTX and I must admit, it's not running well. it seems to run very well on the trailer, no sputtering, no misfiring and good throttle response. This morning I put it out in the water and I had a little difficulty getting it started, because the primer pump is not up to snuff. I squirted some gas into the carbs and it started. But here is what it does: It idles fine I would say. At first it did not want to accelerate when I pulled the throttle, but wanted to stall. After several restarts and careful manipulation of the throttle I finally got it to go into higher RPM doing about 15 miles/hr and then I went to WOT, but the RPM did NOT increase. I was cruising along in WOT doing about 15 miles/h. Engine acted just fine, no misfiring, sputtering, coughing etc. It acted like I was running on half throttle, even though I was doing WOT. Without doing anything else, cruising along at 15 miles/h throttle wide open, about a minute later or sometimes 2 all of a sudden, the RPM starts to pick up and I am doing 30-35 miles/h. and would continue to do so for as long as I don't let up on the throttle. The minute I let the throttle go and then I go back WOT again the same thing repeats. I cruise along at 15 and then a few minutes later it goes into high gear again. I did this for a couple of hours, thinking that everything needs to be exercised and broken in but in the end it would not rev up anymore. It stayed at around 15 miles/h until I turned the engine off. The 15 mile speed is very steady, no pulsating, it almost feels like a speed limiter is keeping it there. I must also add that the doo did not run for 3 years because of other issues, which are all fixed now. There was about a gallon or less of old gas in the tank which was treated before storage. I did treat it again this time and added 3 gallons of fresh 89 octane non-ethanol marine gas to it. I don't think the gas has anything to do with this, but you tell me.
 
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Sounds a lot like the same problem I had with my 96 GTX after carbebuilt. Turns out it was to lean on the low end. Adjusted the idle mxture and the the high end. Runs much better now.
 
Due to other priorities I couldn't got to it sooner. In retrospect I did a good job on the carb rebuild. That's not where the problem was. After fixing myself a triple Southern Comfort on the rocks I did some serious analytical thinking and came to the conclusion that one of the 2 cylinders was not doing its job. One had to overcome the dead weight of the other. I knew that the compression was good, so I started with the most simple and least expensive test. Replace both plugs and make sure they both got fire, which they did. I hooked up the Doo and off to the river I went. Oh boy did that baby go, like a bat straight out of hell. I thought that thing was gonna slip out from under my butt. So this Memorial Day weekend we will spend a lot of time on dog river having a great time. The weather is PERFECT. Nothing can go wrong now! Well let’s hope.
I guess I am going to close the thread, because with y’alls help and good advise all my problems (Sea Doo wise, that is) have been solved. Thanks again and y’all have a great summer. -- Rick
 
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